Re: Zel's Fleet Blog...Citroen, Mercedes, Sinclair & AC Model 70
Posted: Thu Oct 05, 2023 10:41 pm
				
				First job for today was to basically finish putting things back together.
Oil & filter got changed. Which was timed well as I got it done right as a rain shower started, so I was glad to have the bit involving crawling around under the car done.
Reconnected this little linkage which attaches the throttle linkage to the carbs. Getting the little spring clip back on was fiddly. Glad I didn't persist in trying to do that while I was tired yesterday. I'd probably have pinged it off into oblivion never to be seen again.

Coolant was refilled. Using OAT coolant as that's what came out. I'd rather see this using old school glycol coolant, and will probably switch back to that when I change the coolant properly. It's quite murky so definitely wants flushed out at some point soon, this job had only drained about half the radiator, so I was just refilling like for like for now.
Changing the spark plugs didn't happen. Simply because the ones I'd picked up were the wrong size. So I just cleaned up the ones I'd got.
Then reconnected the HT leads, having had the forethought to mark number 1 before I took things apart. Rotor rotation is clockwise.

Before I actually connected the coil I did crank the engine over just to make sure we didn't have any noises coming from anywhere and actually had even sounding compression - which we did. No big obvious skip when it was turning over.
Fast forward a couple of minutes...
https://youtu.be/Ufev94gmCH0
This isn't actually the first start - there's a couple of minutes run time already on there. I didn't have anywhere where you'd have been able to see anything I could have wedged my phone, and I didn't want to miss something important because I was concentrating on recording video.
We did have a couple of coolant leaks initially, one from the lower heater hose and one from the top radiator hose. These are quite old hoses so I needed to ensure the hose clamps were lined up where they used to be. A new set of hoses is on the to do list.
What we also had was a hell of a lot of smoke from the exhaust manifolds. I knew I'd spilled some oil, coolant etc on there while the heads were being removed and the block cleaned etc. However I was quite surprised by the sheer volume of smoke that was generated while it burned off.
Proof the car has moved under its own power again.

Which allowed me to retrieve the things I'd dropped while working on the car. One washer from a carb base, a thousand old exhaust manifold gaskets, and the bolt from the dipstick support. Not bad.
We did a quick bumble round the block. So, so much smoother as you'd expect. Though seemed very hesitant on a light throttle after a minute or two.
Ah.

Initially I figured this was my leak from the top coolant hose having returned, but quickly realised this was actually petrol pouring out of the bowl vent from the offside carb. Yep, that would explain the lumpy running. This is why it's really important to ensure the drain tubes on those ports are properly fitted as it meant this harmlessly drained down onto the ground rather than dumping it over the top of the engine.
Gently tapping the fuel inlet to the carb in a highly technical manner with a screwdriver handle has restored it's continence for now, but I figure they're both probably going to really want a proper inspection and clean. In fairness that carb has been sitting upside down in the boot for the last couple of weeks so it's well within its rights to be a bit grumpy.
Idle speed is quite high, but running a lot smoother now.
https://youtu.be/-oyIrmG-uhc
I'll be doing a little more testing etc over the next couple of days.
After a few heat cycles we will go back and recheck the head bolt torque as things settle.
First trip to an actual destination more than a mile away will be to get the tracking sorted. Currently there is a ridiculous amount of toe out, and that needs seen to!
Hopefully it's onwards and upwards from here.

			Oil & filter got changed. Which was timed well as I got it done right as a rain shower started, so I was glad to have the bit involving crawling around under the car done.
Reconnected this little linkage which attaches the throttle linkage to the carbs. Getting the little spring clip back on was fiddly. Glad I didn't persist in trying to do that while I was tired yesterday. I'd probably have pinged it off into oblivion never to be seen again.

Coolant was refilled. Using OAT coolant as that's what came out. I'd rather see this using old school glycol coolant, and will probably switch back to that when I change the coolant properly. It's quite murky so definitely wants flushed out at some point soon, this job had only drained about half the radiator, so I was just refilling like for like for now.
Changing the spark plugs didn't happen. Simply because the ones I'd picked up were the wrong size. So I just cleaned up the ones I'd got.
Then reconnected the HT leads, having had the forethought to mark number 1 before I took things apart. Rotor rotation is clockwise.

Before I actually connected the coil I did crank the engine over just to make sure we didn't have any noises coming from anywhere and actually had even sounding compression - which we did. No big obvious skip when it was turning over.
Fast forward a couple of minutes...
https://youtu.be/Ufev94gmCH0
This isn't actually the first start - there's a couple of minutes run time already on there. I didn't have anywhere where you'd have been able to see anything I could have wedged my phone, and I didn't want to miss something important because I was concentrating on recording video.
We did have a couple of coolant leaks initially, one from the lower heater hose and one from the top radiator hose. These are quite old hoses so I needed to ensure the hose clamps were lined up where they used to be. A new set of hoses is on the to do list.
What we also had was a hell of a lot of smoke from the exhaust manifolds. I knew I'd spilled some oil, coolant etc on there while the heads were being removed and the block cleaned etc. However I was quite surprised by the sheer volume of smoke that was generated while it burned off.
Proof the car has moved under its own power again.

Which allowed me to retrieve the things I'd dropped while working on the car. One washer from a carb base, a thousand old exhaust manifold gaskets, and the bolt from the dipstick support. Not bad.
We did a quick bumble round the block. So, so much smoother as you'd expect. Though seemed very hesitant on a light throttle after a minute or two.
Ah.

Initially I figured this was my leak from the top coolant hose having returned, but quickly realised this was actually petrol pouring out of the bowl vent from the offside carb. Yep, that would explain the lumpy running. This is why it's really important to ensure the drain tubes on those ports are properly fitted as it meant this harmlessly drained down onto the ground rather than dumping it over the top of the engine.
Gently tapping the fuel inlet to the carb in a highly technical manner with a screwdriver handle has restored it's continence for now, but I figure they're both probably going to really want a proper inspection and clean. In fairness that carb has been sitting upside down in the boot for the last couple of weeks so it's well within its rights to be a bit grumpy.
Idle speed is quite high, but running a lot smoother now.
https://youtu.be/-oyIrmG-uhc
I'll be doing a little more testing etc over the next couple of days.
After a few heat cycles we will go back and recheck the head bolt torque as things settle.
First trip to an actual destination more than a mile away will be to get the tracking sorted. Currently there is a ridiculous amount of toe out, and that needs seen to!
Hopefully it's onwards and upwards from here.




























