Re: Austin, Renault, Rover and more - 02/02 Update
Posted: Fri Feb 05, 2016 6:59 pm
Identified two causes for the non-running of the Princess. The first was the earth wire that was temporarily fixed several years ago. This is one of those repairs where it works so well when done you forget to repair it properly until eventually it fails and you're reminded. The connectors had dropped off the ends of the earth wire in the distributor.

Mike did a beautiful job of soldering new connectors on a new wire (seen here in white) as well as fitting the new condenser.

Initially the car wouldn't start. We pulled a plug to check for spark and at the first hint of a spark the car sprang to life on three cylinders which was quite surprising and unexpected! After everything was all buttoned up properly the car was started anew and seems very willing now. Ignition timing is a little off and the exhaust is blowing as expected. These things will be resolved fairly quickly though I'm not looking forward at all to sorting the exhaust out again.
The other job was to sort out the number plate brackets. I found that if you take the original brackets that fasten between the bumper and valance and turn them 180 degrees they can be mounted to the lower valance quite easily. Only got them stripped back and painted today, we need to drill a couple of new holes to fit them to the car.

Feeling very positive about the car at the moment and I'll gradually work through the electrical stuff that needs attention like refurbishing the headlights, sorting the dashboard wiring properly (a job I've put off for four years) and getting the wiring ready for the new rear lights. It's actually quite exciting to be making progress again.

Mike did a beautiful job of soldering new connectors on a new wire (seen here in white) as well as fitting the new condenser.

Initially the car wouldn't start. We pulled a plug to check for spark and at the first hint of a spark the car sprang to life on three cylinders which was quite surprising and unexpected! After everything was all buttoned up properly the car was started anew and seems very willing now. Ignition timing is a little off and the exhaust is blowing as expected. These things will be resolved fairly quickly though I'm not looking forward at all to sorting the exhaust out again.
The other job was to sort out the number plate brackets. I found that if you take the original brackets that fasten between the bumper and valance and turn them 180 degrees they can be mounted to the lower valance quite easily. Only got them stripped back and painted today, we need to drill a couple of new holes to fit them to the car.

Feeling very positive about the car at the moment and I'll gradually work through the electrical stuff that needs attention like refurbishing the headlights, sorting the dashboard wiring properly (a job I've put off for four years) and getting the wiring ready for the new rear lights. It's actually quite exciting to be making progress again.