Today's adventures start on the electronics workbench.
Our patient was a lovely little Prinztronic Mini7 calculator I picked up about a week ago.
While it powered on there was no response from the keypad (aside from the number 2) and there was clearly an intermittent issue with the power supply.
This isn't a particularly high end calculator...in fact it's very much built down to a price. No screws on the case, it all just clips together.
It is quite stylish though (especially in this two tone blue) and by the standards of the time was fairly compact. Though I'd probably have cursed the dependence on AAA batteries with no DC input jack back in the 1970s...
Took a while to figure out how to get it apart without damaging anything but wasn't that hard really.
No surprises to find a TI TMS series chip at the heart of a calculator from this era - that era being pinned down to mid 1975 thanks to this date code.
There is one other IC in here which I'm pretty sure is just a display driver given where it is in circuit.
Don't recognise that maker's logo. Anyone able to ID it?
The reason for the intermittent power was a dead simple cracked solder joint between a battery post and the PCB.
Easy repair.
The issue with the keypad became self explanatory the moment I started to dismantle it as the metal domes from the keypad switches started to cascade over the desk like metallic confetti.
Those domes should all be stuck to this PCB!
Getting these all back where they were supposed to be was a bit like trying to herd a scurry of squirrels who are all hyped up on Red Bull, but we got there in the end.
I was quite interested to see how the keypad legends were printed...I had assumed the legends were screen printed on the back of the keys themselves. Was quite surprised to find that it was actually just a printed sheet of paper behind the keypad. There are little lenses moulded into the back of the keys which makes the printed text look a little larger.
Quite clever actually. Means they only needed to make one standard type of keycaps for the whole range, just printing a bit of paper to accommodate different layouts or features.
Plus it looks really classy I reckon.
That alone was responsible for my deciding I needed one from this family in the collection the moment I saw one.
Glad to report that it now seems to be fully functional again. I do need to replace the decomposed foam behind the battery contacts, but that's a job for another day. For testing purposes this is absolutely fine.
It is a comically slow calculator though for the period...square root calculations take the best part of 1/2 a second. Division about 1/4 a second...which by 1975 is quite slow. It also doesn't have any logic to stop you taking the square root of negative numbers. It does correctly catch divide by zero though.
The small u at the far left is the arithmetic error indicator on this display.
Should be able to get a page put together for it on the website soon hopefully.
We were then able to move into the garage.
Knowing I was going to need access to the rear brake unions on the flexible lines I needed to remove the rear service hatch again, so decided it was a good opportunity to test something out.
The flashband I'd stuck to it as sound deadening did help, but I don't think it made nearly enough difference to be worth the weight. It pretty much doubled the weight of the hatch. It also added enough extra to the dimensions to make it even more awkward to remove. Additional mechanical noise was being added as well as the insulation never really adhered well to the underside so it was usually sitting directly on the CVT pulley cage.
So today I pulled off most of it (a few areas were thoroughly stuck and weren't going to come off without a huge fight) and gave it a few coats of rubberised truck bed liner.
Several more will be added next time we get a break in the weather. It's already noticeably dulled down the sound of you tap it so mission accomplished hopefully. I'll report back on whether I notice any difference when driving.
The main mission for the day was getting these fitted.
Delivery was once again ridiculously quick from MEV Spares. Ordered at 23:55 on Thursday, parts dropped into my letter box before midday on Saturday.
Nothing particularly complicated here, just fiddly.
I knew I couldn't easily get the union on the back of the cylinder off so didn't even bother. Just pulled it at the Flexi end and planned on feeding the whole lot out through the backing plate in one piece.
Went pretty smoothly. Getting those U clips off the back of the cylinder is a heck of a lot easier when you know how they work! I must have wasted hours on it when I took the first wheel cylinder off KPL, this took me about ten minutes.
Before going any further I made a point of double checking what the threads in the wheel cylinders were *before* I had flared the new brake line... I'd already been very nearly caught out when the master cylinder turned out to be metric. These aren't.
Once I'd suitably plugged the brake line off the old cylinder so it could spray brake fluid into my eye, I was then able to use it to give me an idea how much pipe I needed.
Also checked very carefully to ensure they were indeed as close to identical as possible.
All indications were good.
It was at this stage I ran into a slight snag. These new cylinders are much more of a snug fit through the slot in the back plate. This wouldn't be a problem with the hub on most cars where you can slide it in straight...however thanks to the rather bulky hub on the Invacar you have to slot it in at a slight angle to clear the wheel mounting flange. Just enough to make it bind up. After a bit of head scratching I eventually chose to very gently tap it past the tightest point with a hammer and block of wood. Hopefully nothing was harmed...but short of removing the whole hub I couldn't see an alternative.
I then had a mental foul up and convinced myself I'd fitted it upside-down and spent 20 minutes pulling the cylinder out again to compare to the original. Of course it was absolutely fine so I had to put it all together again.
By this point it was getting dark...and right about the point it got properly dark, my work light decided that this was an ideal opportunity to run out of charge.
Cylinder is in, horseshoe clips are both in, hydraulic line is connected at both ends and the rubber boot is correctly seated around the cylinder and handbrake linkage.
The original pipe had been touching the suspension arm at the lower corner so I deliberately made the new pipe a bit longer so it could be routed better. May see about adding a clip roughly level with the shock absorber to ensure the new pipe can't vibrate.
I really do need to get a wire brush and some paint on that rear suspension at some point, it just looks horrendous.
Sadly thanks to having run out of daylight (it started raining while I was tidying up too), I've a few things left to fit...
No way I was trying to refit those springs in the dark. They're fiddly enough in full daylight, trying to fit them in the dark is just asking to get a spring in the eye!
Hopefully get this side finished and the other one done tomorrow. At least the nearside one I can get to with the car in the garage, offside one requires me to wheel it outside first.